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05.11.20
Fordi aquariet kontinuerlig har vært lekk ble det denne gangen konkludert å forsøke og legge silikon i hele bunnen av aquariet i et forsøk på om dette kunne lage en slags tett film. Denne dagen begynte Fredrik, Gustav og Inge å bygge bordet som aquariet skal stå på. Inge hadde ordnet med materialer. Flere av […]
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Sprint 9
Maskin(Simen): Got to see the 3d prints in action. Found that the bevel gears were not equal to their 3d designed size and didn’t reach each other to connect and spin. I did manage to solve the issue of the missing hub for the stepper motor, although due to size differences from 3d to real […]
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29.10.20
Det ble igjen testet om aquariet var tett, noe det igjen ikke var. Det ble derfor fylt på mer silikon, men denne gangen på innsiden av aquariet. Inge begynte denne dagen å lage vasketårnene til vaskesystemet. Disse ble kuttet ut i kryssfiner. Han 3D-printet også ut komponenter til det samme. Fredrik forsøkte å se om […]
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Seventh sprint – Puck Buddies
This seventh sprint was a bit of a longer one as we have had other subjects we needed to focus on. The following blogpost will therefor include the progress we had the last 1.5 weeks. Anders This week I have finalized our control application for windows, I ended up creating a Windows Presentation Foundation application […]
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Holobot week 44
There has been a rough few weeks for the Holobot team. Overwhelming amounts of school has made putting in solid working hours hard, but after a few meetings and planning we are back on track. We have ambition to have a mechanical working prototype done by Monday 2. October. Log Kjartan Hololens 2 We discussed […]
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Group 2: Card playing robot – Sprint 8
16.10.20-23.10.20 Maskin(Simen): Due to the larger than expected force needed to move the load, we found we needed more than a simple servo as a motor, at least for the base, so we found a stepper motor. While in theory barely providing the Torque needed, we met an unwarranted problem regarding the use of a […]
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Week 9 (19.10-25.10): Automatic watering system for plants
Software (Marius): During this week i have been working on fixing a few bugs in the code, adding more functionality and cleaning up the code a bit. Crane (Servo Motor): I first started with the crane which we want to be moved approximately 80-90 degrees. I first used a for-loop to be able to move […]
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22.10.20
Det ble igjen testet om aquariet var tett, noe det igjen ikke var. Det ble derfor fylt på mer silikon, men denne gangen på utsiden av aquariet. Etter silikonpåfyllingen avgjorde Fredrik og Gustav helt spesifikt hvilke sensorer som vi skulle bruke i aquariet og bestilte disse. Det var en PH-sensor, en vannstandssensor og temperatursensor. Vi […]
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Week 8 (12.10-18.10): Automatic watering system for plants
Mechanical (Shadi and Per-Terje): This week we have worked on the re-design of the battery pack and servo bracket, integrated the smaller parts into the water tank lid cower. We come back to the old design of the water tank to get some more space to further design on. Also, we have started to think […]
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15.10.20
Fordi silikonet skulle bruke 7 dager på å tørke ble det denne dagen testet om aquariet var tett. En test aquariet ikke bestod. Aquariet ble derfor tørket og vi sprøytet på med mer silikon der det var lekk. Silikonet ble sprøytet på innsiden nederst av aquariet.